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HomeMy WebLinkAbout136.39 - Site Plan and Sewage Disposal System (3)i, YAR,MGUTN rsnGV f� Cre r a'4 30 SYSTEM DESIGN :f s.' I, h �:.._....' T. 0 . F , ACCESS MANHOLES TD WlTHN was ed Design Flow: g y Isi ne l/2 3 bedrooms Cc3 //D gal /day 3✓L� ELEV,Sl,v 6. OF FINISHED GRADE Septic Ton k:33D gal. x 200 s 410 goI. 5 Use 1500 Gal Tank ELEV.'�74 S ev > Leaching Facility : USE(,> Svcs CFylcnl C/%�, IT 1' S y,,�4' STONE ��� 46.3 o 3/4-4. 1112 r7 U washed _Bottom: 12- !F Y 33•S )C 6, -?4 s,JI% 641. I` to- sfone j .... ..... c e .e ....... ... ... GA e Sides 2�lZ•8+ 33.5 2x (2, '14 _ 7 G��,�LUNS'\ E 14• BAFFLE ......... esemeEEEE ° e mee®demeeme mmeme®®aame TOTAL J 4 Ga I . ,' ��sNT3 L4e70Vs'e ________�____ 4},3NOTE: Garbage disposal is not Permitted with ` this desi n. 6' crushed stoner under Septic Tank and �� :. �'�• D -Box b'f� 2S'.s �-�r� 4 �i EN61n1EE2-To VEIZtFY -�0)L_S /� pig / ,� ELEV. . 44.E S' SEGac OAn " d?Cun of �EAfilln/E� O��D L CA T /ON Y" !" ELEV . AuuTy RT 77ME cF u�,v ��v f77,W 0 1500 GAL. D -BOX LEACHING` FACILITY aELEv.39.q �� ��° Assessors Map l36 SEPTIC TANK Btm. T.H.�'2 Arree!6 0 �� u Parcel ,324 S.F. 39 Area SYSTEM PROFILE 5. of �o a CONSTRUCTION DETAIL TEST HOLE I TEST HOLE i`2 $Evac TANK LEACHING UNIT STONE nuneT o- EL . 50.5 0- EL. 49.9 ........ . T A LOAMY SAND A LOAMY .SAND '.14' •. eLeor ooc,00Q o0o Op�00 3' 7- I OYR 4/3 6' I OYR 3/1 1 _o4M,j to loon 0000° —± -a B LOAMY .SAND LOAMY SAND ss' �' 102 28--_ cl X58? 0 0 c`� N 28_ w IOYR 5/6 30` B IOYR 4/6 GAS BAFFLE DETAIL N.>.s. 500 GALLON CHAMBER ....... ............... 4' S* r, to .� , 4 , C MEDIUM COARSE C FINE/MEDIUM 120` 1 2.5Y 6/4 120" I 2.5Y 6/4 0 ^ D N0 14A7ERNO WATER h- �jy r J�EWHMAIZ-Y- IS VP NOTES L DATE: JANUARY 18. 2001 pF Y�u_MouTN t�d4D PERFORMED BY R I CHARD JUDD R.S. a 48,9 HYD 1.) SEPTIC TANK `SEAM 13 TO BE SEALED AND W I TNESS : A. -VON HONE , H, A � gouND _ E� EV, S�•4 �'� 6 - WRAP PED : DESIGN RATE: < min , / i n .- C.BASIN / 5 a. Fig � 2 .) ALL AREAS DISTURBED BY CONSTRUCTION 2 1 47. I, 1 ARE TO BE GRADED. LOAM COVERED. 1 i:` AND SEEreD• FNS/ --__ _ i 3) UNSUITABLE I TABLE SOILS ARE TO BE REMOVED FOR Q u PERCOLATION < 48 5104 iso€e vt r i /D s.4 5' AROuNp ;LEACHING AREA AND REPLACED f E R LO L SIT I O N TEST I WfTH APPROVED FILL MATERIAL. 24 GALLONS OF WATER IN 5 MINUTES AND 33 Q G`• IRE �iJ 4� DESIGN ENGINEER TO CERTIFY SOILS REMOVAL SECONDS AT THE DEPTH OF 58 INCHES BEFORE SYSTEM INSTALLATION. 5l511 5:) DESIGN ENGINEER TO CERTIFY SYSTEM INSTALLATION G9�A4E ro o° ' PRIOR TO BACKT:I LL I NG. D scgq, 6:) DISTRIBUTION BOX IS TO BE WATER TESTED AT 7 z _ 45.3 THE TIME OF THE BOARD OF HEALTH INSPECTION. PERCOLATION TEST TH•� co 7.) THIS PLAN IS FOR THE INSTALLATION OF SEWAGE wqR 5 s 9•I DISPOSAL SYSTEMS ONLY AND 1S NOT TO BE USED �- 49'—" FOR ESTABLISHING PROPERTY LINES. PERCOLATION TEST WAVED. STK W SET S� ACCE;y MANHOLES Ar-,5TEM o t3E GENT& -b //v PL<KF 8crOpt ,� w , (J) 5o&0.. T .2 E.VGINEE� WtL� c r Z 49 2. KfIF/ SX57EM /✓51RLLA7 ,V. 48 6 H 45.3 --� PK SET - _ r J 4 9.3 48.8, ,. @ O 47.8: 941 MAIN STREET. SO. HARWICH. MA 42661 To Ll_432-2875 U. P.4 S I TF PLAN SEWAGE DISPOSAL SYSTEM IN YARM0UTP, CB/FND 106,45- FOR 47.8 46.4 I.P./FND 47.6 DEBBIE tpx JOHN DYRD � 2 _FOL L INS POND ROAD YARMOUTH, MA. PROJECT: 01-005 SCALE: 1 30 ` DA TE:3/'/ci