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HomeMy WebLinkAbout46 Pine Cone Drive Site & Sewage PlanA9 16 T.0.F• ACCESS MANHOLES TO W,7T141N s„Qstied SYSTEM DESIGN ELEV 3, D FI EV 6" OF fRNSf D GRADE stance Design Flow; 3 bedrooms 0 110 gal/day - 330 gal A AN ELEV.3 .� Set level first 2' < w o I 1 /[ Septic Tank: 330 gal x200% _ �60 ga 1 • Use 1500 Gal Tank �•p 0 �/s i/v�ns1 Leach Ing FOC 1 1 I ty: Use 0G-} jG•�, L4LLell Lf{�M,L�£1L1 ✓%i`�STDAIE die 14 SEE eeee ee<e e e Q a>ve Bot tom : /7..B zS�XD %61 ��5, = 23.9 •, •_ esavee eoet a DETAIL e=v... SIQe5 7- /7.7,-f- Y2- x01q4-Pa;2 Ap'/ meeeeeveee Use fi' crushed stone ......... •,•,:,...•; ELEV. ZS,D T(DT AL =.3-"y Gal. under Septic Tank and— D-Box 4 pie /% --�- -L' MMI -4n LEV.3 ,"L. S� NOTE: Garbage dlsposoI Is not permitted wlth this design. 1500 GAL SEPTIC TANK D -BOX LEACHING FACILITY +EL.EV. 23.0 44j. cg.01ty SYSTEM PROFILE Not to Boole CONSTRUCTION DETAIL STONE LEACHING UNIT oaoa °v T ooca t�goat okZ � °p0�� 34 �tz tnaaopgoo °D° 7 is L� 102'/ 58' O O o CV 500 --GALLON CHAMBER Pl IVr- COl'��E" ORI vE f�---- 25'- -�-- -----Vis,------ o 30 CAr4H T Aslni C,R ATE ELEV Za,S a p oyes _ 41 — a,t 83,0'0' R 5"Oak. "ff i /r Dg"oak ¢„ ,z Oak- do®z . ry az 3o O B a1c -._ — er3 1 O O 1 30.3 I T 14- 1 5' -PTIC TANK OUTLET ?OW GAS BAFFLE DETAIL N. T. S. , n TEST HOLE _& —EL. 30.1 I I T(ip iw Subsoil 3' — — PERC. Medium to Coarse I I Sand II' — 12' — 5 L 0CA170A1 MAP Pap 7,5A Parcel/ P2 'Oreo'.* C6300-18,,11 NOTES I:) SEPTIC TANK SEAM IS TO BE SEALED AND WRAPPED. 2.) UNSUITABLE SOILS ARE TO BE REMOVED FOR 5' AROUND LEACHING AREA AND REPLACED WITH APPROVED FILL MATERIAL. 3.) DESIGN ENGINEER TO CERTIFY SOILS REMOVAL BEFORE SYSTEM INSTALLATION. 4.) DESIGN ENGINEER TO CERTIFY SYSTEM INSTALLATION PRIOR TO BACKFILLING. TEST HOLE _r 2 EL. 30.2 Subsoil Medium to Coarse Sand II' — 12 ' --- DATE: 3/2/95 PERFORMED BY: Stepphen Moore.S.I.T. WITNESS: Amy Von Hone.B.O.H. DESIGN RATE: <2 min,./in. TEST HOLE 'I'lla DATE_ GERF6RMFp BY: Mar}iv E MDran9,f. WITNESS. Amy Von lone HfA- PESIGN BATF:tam�a�rrch. GROUNDWATER ADJUSTMENT ELEV. 30.3 = A ASO?C/y zca%7 aYRs/3--- i 24 Gallons of Woter in 15 minutes at Q {-f, de th znarriy d'and 9.7' B /d Ye S/d 27— Zon213(3/49'8.1): — Zone B (1 /96- 9.1 ): -3.4'. C /oYz 7/4 4- S4 -- ' Eleu, Z3,D - Elev. 22.6 �p�lllo /Z9 — J09 DATE_ GERF6RMFp BY: Mar}iv E MDran9,f. WITNESS. Amy Von lone HfA- PESIGN BATF:tam�a�rrch. GROUNDWATER ADJUSTMENT PERCOLATION TEST GROUNDWATER AOJ. Groundwater Found : 11' 24 Gallons of Woter in 15 minutes at Q {-f, de th 6roundwa el' Found Index W'ef) MIW-29 9.7' Index Well h11W-29 !9 _ Zon213(3/49'8.1): -2.4` Zone B (1 /96- 9.1 ): -3.4'. 7,3 Adj. G.W. depth - 7.6' ' Eleu, Z3,D - Elev. 22.6 �p�lllo ,,ORAN ENGINEERING, INC. 941 MAIN STREET. SO. HARWICH. MA 02661 432-2878 /lam S I TE PLAN DISPOSAL SYSTEM IN YARMOUM FOR 4b' PINE COME- -40R/VE YAIRI 100TH, MA PROJECT: 9F—Jc:/ "SCALE; / ".jW20 '. DATE::///2l q /kwt hc, sw f*/_,(-