Loading...
HomeMy WebLinkAboutEngineered Plan - 201701 N 4 CLINTON LOCUS LOT0121T(19,063 SF) ASSESSORS MAP: 116 PARCEL: 31 PLAN BOOK: 343, PAGE: 11 C. 0'< 86 M17-30 KEY: EXISTING CONTOUR: - - - - PROPOSED CONTOUR: ------------- EXISTING SPOT ELEVATION: 25.5 PROPOSED SPOT ELEVATION: 25.5 TEST HOLE: * UTILITY POLE: -O- FENCE LINE: HYDRANT: RETAINING WALL: 33.5' co tV LEACH AREA DETAIL 96 SEPTIC SYSTEM DESIGN FLOW ESTIMATE - 4 BEDROOMS AT 110 GAL/DAY=-440 GAL / DAY SEPTIC TANK: 440 GAL / DAY x 2 DAYS = 880 GAL j USE 1000 GALLON SEPTIC TANK (EXISTING) LEACHING AREA: USE 3 - 500 GALLON CHAMBERS (8.5'x 4.8'x 2' EFF. DEPTH) WITH 4' OF STONE ALL AROUND (33.5'x 12.8'x 2' DEEP) SIDE AREA: (33.5' + 12.8') x 2 x 2 = 185 SF (0.74) = 137 GAUDAY BOTTOM AREA: 33.5'x 12.8'= 429 SF (0.74) = 317 GAUDAY `. CAPACITY= 454 GAUDAY j 1, JJ� 1 96.1 3 10 6 3z" F 70' fla .� 98 i th-1 Pole . , o; 94, -11 0 9g ST \ -1 Gaya � �9-qd � <A) I 96.4 X STONE PARKING \ � G 96 94 X92 88-- Shed 8--Shed 90 co . 84 \ /88 N>;6,3,00 \\ BENCHMARK AT LEFT CORNER OF BRICK STEP ELEVATION = 97.21 SEPTIC SYSTEM SECTION 97.50 - COVERS WITHIN 6" TOP OFOF FINISHED GRADE FOUNDATION 94.7 T MAX. COVER ELEV. G 93.65 (1' MIN) (EXISTING) ELEV. 93.9 93.5 ELEV. ELEV. ELEV. F 7.a D -BOX 1000 AL (6" STONE UNDER) SEPTIC TANK TEE SIZES: _(TO BE CONFIRMED) 92.67 INLET: 6" UP 13" DOWN ELEV. OUTLET: 6" OP, 14" DOWN GAS BAFFLE AT OUTLET TEE lr4lo 100 ( 100 S 86°20'22" W �1 BED BED ROOM ROOM BATH 2nd FLOOR BED LIVING ROOM ROOM DINING AREA BED KITCHEN ROOM BATH MUD ROOM 1st FLOOR LIN ROOM DECK ABOVE EXISTING FLOOR PLAN I Yarmouth Health Department AF ' GVED 14a>r>me Date TEST HOLE LOGS ENGINEER: THOMAS McLELLAN, P.E WITNESS: AMY VON HONE, R.S. DATE: 6-7-17 PERCOLATION RATE: < 2 MIN/IN 2" PEASTONE OR FILTER FABRIC - 3/4" - 1 1/2" DOUBLE WASHED STONE INSPECTION PORT i- ELEV.= 93.5 I$811 ° ° 1-1 l 90.67 4 4 ELEV. e 33.5'x 12.8'- > 3 - 500 GALLON CHAMBERS WITH 4' OF STONE ALL AROUND (33.5'x 12.8'x 2' DEEP) TH-1 96.0 FILL ELEV. 30" 93.5 A HORIZON LOAMY SAND 33" 10YR 3/2 93.2 B HORIZON PERC AT 54" LOAMY SAND 60" 10YR 6/8 91.0 C HORIZON MEDIUM SAND 2.5Y 7/4 144" 84.0 NO GROUND WATER ENCOUNTERED NOTES: 1. VERTICAL DATUM: ASSUMED 2. MUNICAPAL WATER IS AVAILABLE. 3. SCHEDULE 40 - 4" PVC PIPE TO BE USED THROUGHOUT SEPTIC SYSTEM. 4. ALL PRECAST UNITS SUBJECT TO TRAFFIC LOADS TO CONFORM WITH AASHTO H-20 SPECIFICATIONS. 5. PIPE PITCH = 1/4" PER FOOT (UNLESS NOTED OTHERWISE). 6. FIRST 2' OF PIPE OUT OF D -BOX TO BE SET LEVEL. 7. THE SEPTIC SYSTEM HAS NOT BEEN DESIGNED TO ACCOMODATE THE USE OF A GARBAGE DISPOSAL. 8. ALL CONSTRUCTION DETAILS ARE TO BE IN CONFORMANCE WITH THE STATE OF MASS. ENVIRONMENTAL CODE (TITLE FIVE) AND LOCAL HEALTH REGULATIONS. 9. CONTRACTOR TO VERIFY LOCATIONS OF ALL UTILITIES PRIOR TO CONSTRUCTION. 10. GROUND COVER OVER ALL SEPTIC SYSTEM COMPONENTS NOT TO EXCEED T WITHOUT VARIANCE. 11. FIELD SURVEY PROVIDED BY TERRY A. WARNER, P.L.S., HARWICH, MA. 12. THIS PLAN REQUIRES THE REVIEW AND APPROVAL OF ONE OR MORE TOWN DEPARTMENTS AND IS SUBJECT TO CHANGE UNTIL SUCH TIME. 13. EXISTING LEACH PIT (AND UNSUITABLE SOIL WITHIN 5' OF PROPOSED LEACH AREA) IS TO BE PUMPED AND REMOVED. 14. D -BOX TO BE WATER TESTED TO ENSURE LEVELNESS AND EQUAL FLOW. RECEIVED 'JUN 22 2011 HEALTH DEPT. SITE PLAN LOCATION: 39 KNOLLWOOD DR., YARMOUTHPORT, MA PREPARED FOR: EDWARD SIMMONS DATE: 6-8-17 SCALE: 1" = 20' BASS RIVER ENGINEERING THOMAS J. McLE LAN, P.E. P.O. BOX 1163, EAST DENNIS, MA 02641 508-364-9048