Loading...
HomeMy WebLinkAbout14 Pleasant Avenue - Proposed Upgrade to Septic SystemGENERAL MOTES.• 1. THIS PLAN IS FOR THE DESIGN AND CONSTRUCTION OF THE SENAGE DISPOSAL FA CIL ITY ONL Y. P. ALL CONSTRUCTION METHODS, MAIEJ9IALS AND MAINTENANCE FOR ME SEPTIC SYSTEM SHALL CONFORM TO MASS, D. E. -O: E. TITLE 5 AND LOCAL BOARD OF HEAL 7 REGM.ATIONS. 3. ALL SEPTIC SYSTEM CGyPONov7s SUBJL'C ro YEHSHALLLBELDES M,EDI TO � rHsrAAj H 2OYLOADING W. ALL SE*M PIPE SHALL BE SCHEDULE 40 OA APPROVED EQUAL. 5, BEFORE STARTING GONS7UCTION CALL DIG SAFE J-800-322-4844 FOR LOCATION OF UNDERGROUND UTILITIES. 6, DATUM IS ASSUMED 7, NO DETERMINA rION HAS BEEN MADE AS TO COMPL 1ANCE ITN DEED RESTRICTIONS OR ZONING REGJLATIONS. IT SHALL REMAIN THE OMER'S RESPONSIBILITY TO OBTAIN ALL REDUIRED PERMITS SPECIAL PERMITS, VARIANCES, ETC. FOR THIS Pl4OJECT. B, IT SHALL REl'INAIN rhF O"EA'S RESPONSIBILITY TO HAVE r1W PROPOSED DMEZLING FOUNDATION DESIGNED TO ACCOUNT fOR ThE EXISTING 6r9ADE AND SOIL COWITIONS AT THE LOCATION OF TIE PROPOSED j9XEZLING. -rW O T3ED ROOM DECO P.ESTP-lCM o,,J ZEnv1 R.ED. Imo) PIPE PITCH- /4,r � UN�5 o-�r`W 1S>~ N D If• Stita✓rDvLe 40 zt" r,vr, P(Fftj� 1-0 13C USEb 12)SySTT,M NOT OESf(rNeO f-02 VSPE or CAp-Bh�e �RIN�lC2. PO INYERT ELEYATIONS.- INVERT AT BUILDING �� • �� INVERT M AT SEPTIC TANK 9s '611.___ INVERT OUT A r SEPTIC TANK�– ZWERT M AT DIST. BOX q `� • SO INVERT OUT AT DIST. BOX 8.33 INVERT IN AT S. A. S. SG BOTMW OF S. A. S. Q3. So OBSERVED 61?OUND)YA7ER N I A ADJUSTED 6X10UNDgA7ER -/Vm CA TCN BASIN RIM = 97.53 ! A �. r • i� 1 MCH - 20 FEET 0 PO do CA TV -1 BASK I RIM = 96..f5 INSTALL A GAS BAFF'_E IN OUTLET TEF • L IOUID ti DEPTH ---� SEP TICGTANK DF -SAW CRMR.TA_ DEC vN F'.OV. dDEO900M DIYFZLINGL 0 110 cSAL/DAY PEA pY1M EOJAI .S - GALS. PER DAY. ACCESS COVERS , ` : - EP MUST TIC T�, BE NK AEOi/IRE7�- 6 4F FINISH GRAOE. 1✓IIXIIN � . .� ,..` 6P9 X 200.E �► COAL. —_ - wpm 9SEPTIC rdh%, PAOYIOETr DIST. IE - BOW • 1-r--• -.:AL .StDTIC TANG' 199 -BOX TO SE SET ON A BE 6F COMPACTED C9U,W "D STONE. ,7GVTR40TCR TO MATER TEST 9-80)( TO S4,0,V LEVELNESS. STONE AL . 3/4"- 1/2' DIA, SIZE OF LEACHING FACILITY REWIRED : 2 k'A D STONE 6L. Q 3 , 50 DEsl&v POW. Rd TE - ?-- MiAvrEs/INC.H PROPOSED S. A. S. ?- GALLONS PER DAY 5#o SIZE OF LEAMING FACILITY PROVIDED.- �o tTon1 0 F rJ TF-5rNoL� U. 88 • io SIL70VALL �!$•° S. F. X ._%.[_ �• $7 -32 -GPD BOTTOM 2-1q,So S. F X ..7y_ TOTALS 332.:56 S• F. SOIL TEST PIT DATA 7'. P. -i 61z"V. REV. � � , I o T. REV 1V1,4 6, W ELEY G, J►: EZEV, D u �7, -,7 Tr`ST BY,• RR A/ jVl7,V SSEI 3Y.• rl • YON lU� l�. ��itR ;go q PERC . RA Ti: 4 '2— NDN. / IN, CLASS I SO I t.._ LT)i` = O. ?y f if TP q` 3 }� r r � I yp tl 0 O FJ/VE C� 1.4/Vb 2. Sy fQ p93.� 1 �� tr Y, 92.77 i2- L �y REVISIONS - AV. DA TE REVISIOtN jH OF �S� DARREN cyG� M. T U MEYER No. 1140 Ok .3 r� 7-6P-iA-t,/ PLAN SHO ?rW A PROPOSED UPMAIDE TO AN EX'.TS T"VG SUBSURFACE SEPTIC D.TSPOSAL SYSTEM . '' R -f L, SANT AEMU,r ; YARMOUTH CACP GROU T YAROUT F 14', SCALE ." " 20 CAUL Y 21, 2003 CANAL LAAO S&MID'. .SOF OLD PL YAlOU7H 1OAZ7, 5,4 �',4MORE SERC , N PROJECT 11,,425 -03--05.