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HomeMy WebLinkAboutEngineer Certification Letters (p�� n D I nSCHOFIELD BROTHERS E ENGINEERING • SURVEYING • PLANNING NOV 1 4 1995 Schofield Brothers of New England, Inc. November 7, 1995 161 Cranberry Highway HEALTH DEPT. P.O.Box 101 Orleans,MA 02653-0101 508/255-2098 or 508/398-3311 FAX 508/240-1215 Town of Yarmouth Health Department 1146 Route 28 South Yarmouth,MA 02664 Attn: Bruce Murphy Re: William Coldrick, Septic System Installation Lot 5,Smiths Point Road, Great Island, West Yarmouth,MA Dear Bruce: On Thursday, October 26, 1995,this office performed an inspection of the installed sewage system septic tanks and related equipment at the referenced site in order to certify to a satisfactory installation. At that time,we made a recommendation that the sanitary tees in the septic tank on the west side be trimmed to the lengths as called for on the septic plan. We understand that this was done. Also at that time, a recommendation was made to provide a more practical cover for access to the septic tank on the east side. We do not know if this was done, however,we presume it was. None-the-less,we wish to certify, based upon the inspection made on October 26th combined with our inspection results of 1993, that the sewage system has been installed in conformance with the plans as approved. Please don't hesitate to call me directly should you have any questions. Thank you for your cooperation with the project. Very truly yours, SCHOFIELD BROTHERS of NEW ENGLAND, INC. Robert . Perry, P. . RMP:mkr 0-8624 0o SCHOFIELD BROTHERS ENGINEERING•SURVEYING•PLANNING 161 Cranberry Highway P.O.Box 101 Orleans,MA 02653-0101 _, _. 508/255-2098 �; FAX 508/240-1215 [2 l. '..rA ,N^ December 14, 1993 DEC 1 6 1993 HEALTH DEPT. David Mason Asst . Health Agent Yarmouth Health Department 1126 Route 28 South Yarmouth , MA 02664 Re : Coldrick Leaching System Excavation 63 Smith Point Road , Great Island , West Yarmouth , MA Dear Mr . Mason : On December 9 , 1993 , we inspected the above referenced excavation . The installer had done an exceptionally good job of removing the unsuitable material for 10 feet around the proposed leaching system to a depth of approximately 9 ' at the southeast side and approximately 12 ' on the northwest side . In the excavation , the contractor temporarily opened a hole down to elevation = 2 , 4 feet below the proposed bottom of the leaching system. We encountered clean , medium fine sand to satisfy Note 17 on the proposed sewage disposal system plan concerning soil quality verification below the leach pit . Very truly yours , SCHOFIELD BROTHERS of NEW ENGLAND , INC . a,----- ; J . Dan Bremser Project Manager JDB :mkr 0-8624