Loading...
HomeMy WebLinkAboutEngineer PlansNKEY: 4 EXISTING CONTOUR: - — — - PROPOSED CONTOUR: ......... EXISTING SPOT ELEVATION: 25.5 PROPOSED Y SPOT ELEVATION: 5.5 TEST HOLE: UTILITY POLE: -o- FENCE LINE: - HYDRANT: -6- RETAINING WALL: LOO 3TI(1876 TSF) ASSESSORS MAP: 99 PARCEL: 45 LAND COURT CASE 31209 COME mim Ommmm11 rj ONLY, due to ~lair and I. -,al septic variances. :.Board of IIrallh ... ur, and y,proval o required for any. Iul";t ad.t,lwm+u i„„il,oln.aitr,:Ilioru to seware la, hoes Of,., ,rsHh+rllml;. I xrnl.uoh Ilvahh U,rparruu•uf Name4 Dale II4TA 105 103 104 10\..�� ,.,.. 7L / BENCHMARK AT — LEFT CORNER OF BRICK STEP ELEVATION = 104.84 E I AT 110 GAL / DAY = 220 GAL I DAY SEPTIC TANK: 220_ GAL / DAY_L2_ DAYS= 440 GAL USE 492Q GALLON SEPTIC TANK (EXISTING) LEACHING AREA: (3 BEDROOM, MINIMUM DESIGN) USE 24 INFILTRATOR QUICK HIGH CAPACITY CHAMBERS °w SIDE AREA: NA (0.74) =±!A GAL/DAY BOTTOM AREA: 4'x 24 UNITS x 4.7 = 451 SF (0.74) = 3 AY CAPACITY 334 4JDAY 105 SEPTIC SYSTEM SECTION (.OVFRR WITHIN A BED BATH LIVING ROOM I ROOM ROOM AAIRNEAG KITCHEN (EXISTING) ELEV. LI, 1000 GAL �T SEPTIC TANK INLET: 6* UP, SBDOWNFIRMED) OUTLET: 6" UP, 14" DOWN 1/8' per It 14 118"oerft_ D -BOX (6" OF STONE UNDER)✓ -GAS BAFFLE AT OUTLET TEE TEST HOLE LOGS PATIO ENGINEER: THOMAS MoLELLAN, P.E. WITNESS: MALLORY ANGLER, R.S. DATE: 4-2-20 PERCOLATION RATE: < 2 MIN/IN I EXISTING FLOOR PLAN I N \\ /• GP 103 \ DRIVE \ \r \ \ _ 102 \ \ f 101 r \ ._.. 100 \ ` 101 `des' 100CA 00 TERRY ANN WARNER No. 38721 NOTE: 8" INVERT INLET IS I THE CENTER INLET OF ENE 4 PORT'" ELEV.= 1C 1E00.1 e 35' x 9' USE 4CAPACITTYY INFILTRATOR QUICK AS SHOWN (35' x V x 8" EFF. DEPTH) THA 104.0 B HORIZON LOAMY SAND 10YR 5/8 101.7 Cl HORIZON PERO AT 48" MEDIUM SAND 2.5Y 7/4 1 NO GROUND WATER ENCOUNTERED NOTES: 1. VERTICAL DATUM: ASSUMED 2. MUNICAPAL WATER IS AVAILABLE. 3. SCHEDULE 40 - 4" PVC PIPE TO BE USED THROUGHOUT SEPTIC SYSTEM. 4. ALL PRECAST UNITS SUBJECT TO TRAFFIC LOADS TO CONFORM WITH AASHTO H-20 SPECIFICA- 5. PIPE PITCH = 1/4" PER FOOT (UNLESS NOTED OTHERWISE). S. FIRST 2' OF PIPE OUT OF D -BOX TO BE SET LEVEL. 7. THE SEPTIC SYSTEM HAS NOT BEEN DESIGNED TO ACCOMODATE THE USE OF A GARBAGE DISP S. ALL CODE CONSTRUCTION FIVE) IIN DETAILS ARE HEALTH E IN CONFORMANCE WITH THE STATE OF MASS. ENVIR01 9. CONTRACTOR TO VERIFY LOCATIONS OF ALL UTILITIES PRIOR TO CONSTRUCTION. 10. GROUND COVER OVER ALL SEPTIC SYSTEM COMPONENTS NOT TO EXCEED 3' WITHOUT VARIAI 11. FIELD SURVEY PROVIDED BY TERRY A. WARNER, P.L.S., HARWICH, MA. 12. THIS PLAN REQUIRES THE REVIEW AND APPROVAL OF ONE OR MORE TOWN DEPARTMENTS AN REPRESENT A FULL DETAILED PROPERTY SURVEY. 13. EXISTING LEACH PIT IS TO BE PUMPED AND FILLED WITH SAND OR REMOVED. 14. D43OX TO BE WATER TESTED TO ENSURE LEVELNESS AND EQUAL FLOW. THOMAS J. McLELLAN CIVIL No. 36471 11 V1VWI Ivy VV E � THOiAAS J. McLELL , P.E. APR 16 HEALTH I SITE PLAN LOCATION: 136 ASTOR WAY, S. YARMOUTH, Mf PREPARED FOR: STEVE & ANNE PALADINO DATE: 4-3-20 SCALE BASS RIVER ENGINEERING P.O. BOX 1163, EAST DENNIS, MA 02641 508-364-9048